The LMS-1 well at Lalla Minouma (SDX WI: 75%) encountered 16.4 m net gas pay in high quality sands (32% porosity) in an over-pressured section in the H-9 sequence that had not been previously tested in the area. In addition, the cuttings showed evidence of fluorescence indicating the potential presence of liquid hydrocarbons. This completes a drilling campaign in Morocco comprising of seven successes out of nine wells or a 78% rate of success. We have assumed the discovery is around half of t
09 May 2018
LMS-1 completes successful drilling campaign in Morocco
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LMS-1 completes successful drilling campaign in Morocco
SDX Energy PLC (SDX:LON) | 3.6 0 0.0% | Mkt Cap: 7.36m
- Published:
09 May 2018 -
Author:
Stephane Foucaud -
Pages:
5
The LMS-1 well at Lalla Minouma (SDX WI: 75%) encountered 16.4 m net gas pay in high quality sands (32% porosity) in an over-pressured section in the H-9 sequence that had not been previously tested in the area. In addition, the cuttings showed evidence of fluorescence indicating the potential presence of liquid hydrocarbons. This completes a drilling campaign in Morocco comprising of seven successes out of nine wells or a 78% rate of success. We have assumed the discovery is around half of t