• The State 36-2 well achieved peak rates of 2,848 boe/d, including 856 bbl/d of oil, on a small 18/64 choke. During a separate, 48-hour phase of testing on an 8/64 choke, production ranged between 700-1,066 boe/d, with 200-400 bbl/d of oil. Importantly, there was no material drop in bottomhole pressure in either test, confirming that sustained production at these levels is feasible long-term. Zephyr highlighted that well deliverability is more than sufficient for commercial operations.
• In add ....
07 May 2025
Zephyr Energy Plc (AIM: ZPHR): Well test success unblocks the Paradox
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Zephyr Energy Plc (AIM: ZPHR): Well test success unblocks the Paradox
Zephyr Energy PLC (ZPHR:LON) | 2.6 0 0.0% | Mkt Cap: 54.6m
- Published:
07 May 2025 -
Author:
Stephane Foucaud -
Pages:
5 -
• The State 36-2 well achieved peak rates of 2,848 boe/d, including 856 bbl/d of oil, on a small 18/64 choke. During a separate, 48-hour phase of testing on an 8/64 choke, production ranged between 700-1,066 boe/d, with 200-400 bbl/d of oil. Importantly, there was no material drop in bottomhole pressure in either test, confirming that sustained production at these levels is feasible long-term. Zephyr highlighted that well deliverability is more than sufficient for commercial operations.
• In add ....